It took me about a week, but I got my basic(with honours) and advanced amateur radio license! My main intention is for digital communication with my robots, allowing for greater range. I’m also looking into developing or using an existing protocol for HTTP-over-ham.
A few months ago, April, I think, my local university was giving away two tape libraries, model IBM Totalstorage 3584. I had to leave one behind, but I was able to convince my parents let me get one. They weigh 900 pounds and are huge, so I rented a uhaul. A friend, my dad, and I spent an afternoon moving it home.
I’m on the right. This is a picture my dad took of us after we got it in the truck. It’s a pretty good indicator for the size of the beast.
Fast forward to last week, and my parents made me throw it away. I kept the drives(LTO3 and LTO4), the power supplies for them, and most of the electronics.
I started with the power distribution unit(PDU). It was held together with rivets, and when I tried to drill them out, they just spun. I tried to burn them away with hydrochloric acid, but I partially filled my basement with chlorine gas, which was a bad idea. In the end, I used a motor from a drill without the gear box, and grinded them away. It worked really well, and I had it apart in under an hour.
Here’s what’s left of the PDU. I intend to take out the screw terminal block in the future. Inside were 3 very hefty relays. They make a very satisfying “ca-chunk” sound. Furthermore, there were 2 hot swappable 37V 290W power supplies. I could take them out without opening the PDU, but I wanted the connectors for them as well. The tape library uses a lot of power, so it has its own dedicated set of circuit breakers – I took them out too. Two are rated for 15 amps, and one is rated for 30 amps. There was also an extremely overkill 36 volt, 1.2 amp fan. I can feel it blowing from roughly 10 feet away!
Now onto the heart of the machine – the robot. Most of the value of the tape library was in it, so I was curious what was inside. I did try to get it running, but without any schematics, it was difficult. It did turn on, but wouldn’t move. I even tried looking for a serial connection on it, but eventually gave up.
Let’s start with the motors. They were certainly big, but what I found interesting is the variety of motors. The biggest one controlled the vertical motion of the robot. It was connected to a 4 foot lead screw via a pulley. The next biggest motor controlled horizontal movement. It was also connected via a pulley, but to a wheel that could ride a track instead. These two motors had their own dedicated motor drivers, which I intend to use with an Arduino. They’re also brushless motors, with three wires to drive. There was also some kind of filter board, which the drivers and motors plugged into.
The next two biggest motors were used in the tape grabber. The machine could grab two tapes at once, which is why it has 2 motors – One for each grabber. These are just standard DC motors. Finally, the last motor was used to turn the grabber assembly around. Tapes would be mounted on both sides of the inside, and there’s a barcode reader on the opposite side, so it was important for it to be able to turn. What’s interesting is that this is the only motor that has a gear train on top. It’s also brushless, but I wasn’t able to find a driver, or even a chip with a heatsink, anywhere.
The barcode scanner came out, and it looks like it would be easy to interface with an Arduino.
All the motors were equipped with some kind of encoder on the end, which fed back into the board for extremely accurate positioning. There were also endstops on some parts of the robot. Overall, it’s a very nice piece of engineering.
I have absolutely no idea what I’m going to do with any of the parts, but I’ll probably sell most of them.
A few days ago, there was a post on /r/Minecraft. Someone put up a 1.4GB world file. It was a scale model of the Earth. It got more popular than they expected, and they hit bandwidth limits on free sites, so I offered to host it for them, with no limitations. It peaked somewhere around 85 downloads. Although my internet upload was saturated, I didn’t really mind. By the next morning, I was down to only 5 or 6 concurrent downloads(I keep a window open on one of my screens that checks every 2 seconds). I thought my 5 seconds of fame were over.
But then the concurrent connections count started rising again. Within a minute it was back up to 20, then 30, then 40. I was extremely baffled, so I thought to google the link to the file on my server. It led to the description of a youtube video, which had been posted 15 minutes ago by this point. I checked and he had just over a million subscribers! The download count kept rising, up to 118 concurrent downloads.
I didn’t mind, but there were a few problems. First of all, I didn’t want the file hotlinked, so I set up a rewrite rule(301) to redirect from the file(Which was hotlinked on a different domain, a website purely dedicated to silly things my math teacher says) to a page on my blog, with a link to the file in the post. It was a pretty short post, the youtuber was french so I didn’t want to hide the download link too much. I had that fixed in a few minutes, but I still had another problem.
The server was taking 4-5 seconds to load the math teacher site, which was purely static HTML and an image, and was timing out to reach my blog(WordPress + https). The CPU and RAM of the web server weren’t anywhere near maxed. It turns out the problem was in apache’s config: “MaxClients” was set to its default of 150. I increased it to 500, and immediately, load times went away, and everything was back to normal. Apache2 peaked around 180 processes, if I remember correctly.
This was all yesterday. It seems to have died down now. I made a dollar from adsense for all my hard work. c: (Kidding of course, it was a lot of fun for me, especially having my homelab being used by so many people, and I’d gladly do it again!)
I’ve spent the last week on-and-off building a robot so I could remotely watch my house when on vacation. What I’ve built is hugely overkill, but it works great and it’ll be easy to repurpose in the future. It has a massive LED on the front, way too much torque, a Linksys WRT54G for transmitting and receiving data, and an Arduino Mega 2560 as a brain.
Let’s start with the motors. I am using two drill motors. I bought the drills at Value Village, a local thrift store, for roughly $5 a piece. They weren’t the same voltage, so I have to use software so the robot doesn’t drift. They are extremely powerful; The robot was able to pull around a cart with a very heavy marine battery on it. I could probably pull more, but the limitation was that there wasn’t enough weight above the wheels, so the wheels would spin. I have the motors software limited to roughly 40% of their maximum power, because at 100% they’re incredibly fast.
For the motor drivers, I’m using a pair of BTS7960’s. With a maximum current of 43A, they are massively overkill for the drill motors. Both motors together, when stalled, draw around 10 amps. I imagine if the put the throttle at 100% I might get closer to that 43 amp limit. When driving the robot, the heat sinks don’t even get hot. Because of my frugality, I previously tried to use relays, in an H-Bridge, to drive around. It would have worked, if it wasn’t for the motors being way too fast at 100% power.
On previous robots, I’ve always had a problem with traction. This was due to using wheels from things that were designed to be pushed, for example, the wheels off a stroller. I’ve solved that problem – About a year ago, I saw a very hefty R/C car at the side of the road. I’ve kept the wheels, the motor, and the servo, but threw out the chassis. The wheels are also very hefty, and have no problem getting a grip. One slight problem I have is there isn’t enough weight above them, so they have a tendency to spin.
To mount the wheels to the motor shaft, I had to use a 3D printed part. At first, I just had the shaft screw into the part, but they kept shattering, so I found locknuts to go on the end of the motors, and I designed a part that could fit the lockut. The other end of the part has a few mounting holes – extras, even – and the wheels mount with two screws(which is a lot more secure than it sounds)
The robot also has a flashlight. I used a 30W LED and driver, which is way overkill, but it’s just what I had lying around. (I used it on my bike at night once, with a lead acid battery strapped to the side, and I lit up the entire width of the street and then some!) The driver is just an adjustable step-up converter, rated at 150W. It’s controlled by a 2 channel relay, giving me an extra channel for later.
Oh, and this robot actually has a proper fuse box, which is better than what I used to do, which was to just not mess up. Each motor has its own fuse, the LED has its own fuse, and the final fuse is for all electronics. I probably should have added another fuse between the battery and the power distribution screws, which provide power to the fuses.
For power, I have chosen to use a modest 12V 7AH lead acid battery. I put it right above one of the motors, which helps greatly with traction. I might upgrade to 2x 18AH 12V batteries, one above each motor, but for now, I still get about 2 hours of battery life. I also have a trailer with a marine battery, which should give me a lot more battery life once I add some weight above the wheels.
Power management is interesting. There are two very thick wires between the battery and two screw terminals – One negative, and one positive. There are 4 wires coming off the positive screw. Each goes to a different fuse. There are 6 wires coming off the negative screw, since some fuses have more than one device attached to them. There’s also a USB battery on top of the robot. This is to power the IP camera. While there’s no reason not to get a 12V to 5V converter and connect it to the same source, there’s also no reason to change. The battery is basically weightless, since it’s lithium based, and it runs longer than the lead acid. I had a 12V to 9V switching regulator laying around, so I used it to power the Arduino, to raise its efficiency slightly higher than it would be if I just fed it 12V.
What I’m sure you’ve noticed is that there are two layers. I actually physically ran out of space on the first layer, so I had to add a second layer. They are separated by 4 3D printed parts. I could have used wood, and it would have been stronger, but I have to cut all wood with a handsaw and it was a lot easier just to design and print instead.
I wrote all software myself, from scratch. Actually, that’s a lie, I borrowed some code from previous robots, but I improved upon it a lot for this version. First of all, the software was originally designed to run on a much smaller robot, which meant there were no safeguards. For example, if the robot was going forward and the connection dropped, it would keep going forever. I was able to fix that in this revision, so if no command is received for 250ms it cuts the motors and the light. It’s also able to gracefully recover from an unclean disconnect, instead of requiring a reset, which wouldn’t have been good if I was 1000 miles away. If no command is received for 2500ms, it terminates the client, allowing for it to start looking for another. Oh – and if one person is driving the robot, it doesn’t allow any other connections.
In conclusion, this robot will easily serve its purpose, and then some. I spent around $100 CAD on it in total, which is a very modest price for such a powerful machine. If I had a chance to redo it, I would have given it some slightly bigger batteries, and I would have positioned them above the motors to give me more torque. After attaching a blade to its bottom, it should make a very good autonomous lawnmower.
While browsing Thingiverse, a 3D model hosting site, I stumbled upon this. It’s a betavoltaic cell, meaning it generates electricity from a source of beta waves. In this case, beta waves are generated from a small vial of tritium gas. The beta waves excite phosphorous, coated on the vial, which powers a small array of solar cells. Tritium-fueled betavolatic cells can provide power without intervention for up to 20 years! I found some flaws in his design, though, so I’m designing my own.
The main problem with the design I found is that it uses extremely inefficient solar cells. The cells only have about 45% of their surface area as photovoltaic material, meaning the rest is wasted. The tritium vial puts out minimal light, so every photon counts. Furthermore, I wasn’t able to find a panel of the same size that would still fit, while using the full surface area. My design uses these. They aren’t much bigger, but have 5 times the power output, which is a colossal difference.
There is still research to do before maximum efficiency can be achieved.For example, at what light level do the solar cells perform most efficiently? The more panels are put in a betavoltaic cell, the less light each one gets. If their efficiency was perfectly linear, it would even out, and the betavoltaic cell would generate the same amount of power no matter the number of solar cells, so less solar cells would be better due to the reduced cost. However, this is the real world, and nothing is ever that perfect. Solar cells will have a peak efficiency at a certain light level. That peak efficiency determines the ideal number of cells.
The files to make your own can be found on my git server.
While looking for an old project on my hard drive, I happened to stumble upon a different project – A Kinect-enabled green-screen that I wrote months ago. The idea is it uses a user-defined threshold to determine what pixels to replace. The default is 2000mm, or 2m. Any pixel closer than that is counted as ‘foreground’, and the corresponding background-image-pixel will be replaced with the pixel from the Kinect camera. This method has a massive advantage: No special lighting, background, or equipment is needed. Not even a flat wall is needed!
Of course, I wrote the program as a proof of concept more than anything. As such, there is no option to record – It just presents the modified image in real time. In fact, many variables that are now customizable through the GUI could only be changed within the code before I rediscovered the project and decided to improve it slightly.
I’ve started working on a new project, to shoot down quadcopters and drones, primarily using an Xbox 360 Kinect. The idea started as a joke back in 2014, shortly after Amazon released its Amazon Prime Air video that went viral. A friend and I came up with the idea, as a joke, of course, to go after the drones for their items. Finally, a few weeks ago, I remembered that idea and thought it would be fun to build it.
Although it isn’t finished yet, it uses 2 nema 23 stepper motors, 2 stepper motor drivers, an Arduino Mega(way overkill) and a 24V 10A power supply. I had all these laying around from a previous project which didn’t work out. Eventually, I plan on attaching an EMP device, although the original plan was to use a HERF gun. The reason I changed my mind is because an EMP isn’t harmful against humans, and also allows me to release a lot of energy in a burst. Also, I’m going to mount a Mini ITX board on it, because right now I have to connect it to my desktop whenever I want to use it.
I wrote the code from scratch in C#. It communicates via Serial to the Arduino and uses the Kinect SDK. Furthermore, it has a graphical interface that allows me to see what the kinect sees, and also shows if it’s moving up, down, left, right, or is in the correct position already. Basically, it finds the object that is closest that is still within $minDist and $maxDist, and moves the Kinect accordingly so it is within $threshold of the center. These are the only 3 configurable variables.
I designed the frame myself, and 3D printed it. The frame mounts onto a large wooden stand that I found in my basement. It’s very sturdy, and if a part ever breaks, I can just print a new one!
The total cost of this project, so far, would be around $150, but with more appropriately sized parts, it would be possible for less than $75. These figures are in CAD and they only include the electronics/the motors. Of course, the EMP device is what will cost the most, due to the capacitor bank it will need.
I don’t ever plan on using this on drones, because that would be extremely illegal and a terrible idea in general. This is nothing more than a proof of concept and should not be attempted.
Here are some pictures and a video in operation. Due to the clutter in my room, it kept losing focus on me. Outdoors, it works much better, which is where it will be operated anyway.
Update: I have uploaded all the files to github. Currently, it is going through a major redesign. Also, I’ve created a page on Hackaday.io.
3D printers are amazing machines. They can take spools of plastic, and make virtually anything you want. But the real question is, can they cook toast?
Hi all. I had an old heated bed and matching glass that I temporarily used when my 3D printer was out of order. In theory, it could reach a temperature of 130C. Would this be enough to toast bread?
I attached some spade connectors onto the heated bed wires, which I had attached previously. Connecting the whole thing to a SLA battery, I could quickly feel it heating up. I used a piece of glass to keep it from heating up the counter top too much.
So, how did it work out?
After leaving it on the bed for around 20 minutes – 10 minutes on each side – I tried out the toast. It was warm on the outside, but the inside was still ice cold. So, unfortunately, I ended up with only slightly toasted bread.
If I wanted to improve upon my toaster, I would sandwich the toast between 2 heated beds, and I would put something heavy, like a brick, on the top. This would ensure good thermal contact, and would also keep the heat in. I think it could have worked out that way, and it would half the toasting time – the bread wouldn’t have to be flipped.
I bought a 3D printer! I purchased it from Newegg. With tax and shipping, it cost roughly $588.
I got the Davinci 1.0a. According to the internet, it has a few minor problems that could easily be fixed. When I got mine, I didn’t have any problems and it worked perfectly. Still, I installed Repetier firmware so I could use my own filament rolls.
I have ordered a 1kg each of red, orange, green, and glow in the dark filament.
Already, I’ve printed out a calibration board, a key chain, a pan/tilt servo camera mount, and replacement parts for the 3D printer in case it breaks. Currently, I am printing a spool holder for the extra spools, which are supposed to arrive tomorrow.